Depyrogenation Study

DHO Step Removal

Project

Description
1

Cleaning failures limited to 5% of systems (inherent design issue).

2

Cleaning turnaround reduced to 32 shifts (multi-stranded).

3

Operational savings of ~ €3.75 million per cleaning operation.

4

Batch capacity increased by 27 per annum.

This endotoxin reduction study was performed at the Hyde Analytical Laboratory using a Charles River MCS150 Endotoxin Analyzer and Getinge Life Science 910 LX Ultima parts washer. 

Recovery of endotoxin indicator from glassware was evaluated following development of a spike and rinse method.

The study was then scaled to larger glassware, and finally confirmed following cleaning in a parts washer using cycle parameters representative of full-scale. Confirmation was performed using several load configurations and two cycles.

Cycle development of the laboratory parts washer was performed prior to chemistry and load geometry confirmation, and included cycle parameter programming and spray coverage testing.

Finally, the study was transferred to the client site for use in cleaning validation for glassware.

Solutions,

Results and Accomplishments
Phase I

Developed a spike and rinse method for recovery of endotoxin from glassware, including scalability testing using a range of endotoxin concentrations. 

Phase II

Evaluated cleaning process parameters with multiple chemistries and load geometries to confirm removal of endotoxin.

Phase III

Transferred the endotoxin recovery method to an on-site Hyde engineer for execution during parts washer validation.

Scope

and Deliverables

Study

Overview

Dry heat ovens are commonly used for depyrogenation in pharmaceutical manufacturing, which is the process of removing pyrogens (usually endotoxins from bacterial cell walls) from equipment or packaging materials. The ovens need to maintain a consistent temperature for extended periods, which can lead to relatively high energy usage. To reduce energy consumption and better characterize cleaning steps, drug manufacturers may leverage endotoxin removal studies during cleaning validation. Removal of the widely used DHO step has the potential to significantly improve environmental impact and save on costs. 

Glassware used for storing bulk materials is cleaned within parts washers using a validated cleaning cycle, including a dry-heat oven depyrogenation step. This study was conducted to evaluate removal of endotoxin from glassware without the use of the DHO step. Studies indicate sufficient endotoxin reduction is achieved without the use of the DHO step, demonstrating promise for site-wide removal of this step following formal parts washer validation at a large U.S. manufacturing site.